Our Oka is our Lifeline

On our outback treks, our Oka is our lifeline.

To fully enjoy our travels, (as in the photo above of a delightful campsite in Lakefield National Park), we need to constrain the risks inherent in outback travel, whilst providing a reasonable degree of travelling comfort.

Like all vehicles that are subject to harsh conditions on rough outback tracks, Oka's need to be well equipped and maintained, and although they are very tough vehicles, they can and do break, hence the need for "Travails", or engaging in painful or laborious effort.

These articles describes some of our travails: how we've fixed failures, avoided problems, and upgraded the facilities on our 4WD Oka motorhome. See the full list of articles in the right sidebar.

Monday, November 8, 2010

Fixing the Leaking Steering Box

As we travelled the rough roads across the Gulf Of Carpentaria from Burketown to Booroloola, we noticed a drip of red oil from the power steering box. Checking the hydraulic fluid level revealed that the level had gone down about 1 inch. There was nothing that could be done on the side of the road except to top up the reservoir and carry on, mindful of the fact that on a Oka, the power assistance for the brakes also comes from the same hydraulic power source as the steering, so a loss of hydraulic pressure could be quite serious.

By Booroloola the leak had got worse and was traced to the seal around the input shaft on the top of the steering box. After a long search, we bought a 4 litre can of fluid from a mechanic in Boorloola, the last fluid in the town it would seem.

[Note: After doing this fix, it appears that that a major steering failure from a leaking seal on the input shaft is unlikely, unless the reservoir runs dry].

Red fluid oozing from the steering box.
On the stretch from Booroloola to Katherine, the leak stabilised but it was still losing about 250 ml a day, but what was worse was that the fluid dribbled down the outside of the steering box and was then liberally sprayed by the wind over the chassis, springs and eventually down the side of the Oka where of course the dust stuck to it, creating a sticky mess. We covered the steering box with a modified wine cask bladder to stop the dispersion of fluid but something permanent needed to be done, which could only happen after got home a month later.

The Fix

The steering box fitted to later Oka's (or as an Oka mod to replace the earlier Kirby-Bishop steering box) is a TRW TAS-30 box made by TRW Torfinasa, Spain. You won't find much data on this model which was fitted to a number of European small trucks. However, it is similar in style and operation to other TRW TAS series boxes so information on the TAS-40 to TAS-85 range is quite relevant.

The TRW identification label.
There are a number of useful TRW articles on their website which document the process of replacing the input shaft seal on a TAS series steering box. Even though none of them specifically relate to the TAS-30 steering box fitted to Oka's, these are the most relevant:

TAS Series Service Manual TRW1108 (more detail than you'll ever need)

Service Procedure TAS100 (On-vehicle repair procedures)

Input Shaft Resealing Instructions TRW800 (Useful descriptions with colour photos)

Replacing the input shaft seal can be done without removal of the steering box and takes the best part of a day, once you have the bits and understand the instructions. There is no need to remove the pitman arm or any other components under the vehicle


In a nut shell, you'll need to:


1) remove the radiator grille and LHS headlight frame, and unplug/move aside any cables which will get in the way,


2) remove the steering column shaft, including the lower UJ. (You can do this without removing the steering wheel housing by slitting the rubber boots to remove them and gluing or clamping them back together later. The metal top clamp and foot can also be cut to aid removal and refitting. Refer to our blog entry here for some details on this),


3) prepare for some fluid spillage (you might loose half a litre or so, it doesn't sound much but it can spread a long way),


4) thoroughly clean the top of the steering box,


5) remove the dust/dirt seal from around the input shaft, it's just clicked into a groove on the input shaft,


6) remove the internal circlip (or flat spiral spring clip in our case) from its slot above the seal,


7) temporarily replace the lower UJ on the input shaft and loosely fit a pinch bolt,


8) disconnect the hydraulic return hose from the steering box (it's the larger fitting and marked "R", see the photo below to ensure you get the correct one) and quickly cap the return outlet to avoid fluid loss,


9) quickly plug the end of the return hose,


10) tie an old piece of towelling around the shaft to contain any expressed fluid,


11) spin the engine for a few seconds but don't allow it to start (disconnect the wire to the fuel cut off solenoid on the injector pump). This builds up pressure in the hydraulic system and pops out the seal. Refitting the UJ prevents it shooting skywards. When you hear a "pop" as the seal pops out, stop spinning the engine immediately to reduce fluid loss.


12) remove the UJ and towelling and the old seal. The old seal was not damaged but the sealing lip had completely worn down (compared with the new one) and was barely making contact with the input shaft.

[There is actually not a lot of pressure behind this seal in normal operation, the real hydraulic pressure is directed to the steering rack pistons during a turn operation, or is simply returned to the reservoir (unless the return port is blocked, as when the seal is being forced out). So I think there was little risk of a major steering failure unless the reservoir ran dry.]

13) clean up the top of the steering box and reinsert the new seal, spring side downwards, grey side upwards. (This requires a special tool, plus some care to avoid inserting the seal too far. You can easily make a suitable tool, see notes below).

14) fit the new circlip, ensuring that it is fully in its slot,

15) reconnect the return hose and tighten fully,

16) bleed the system if required (it has an automatic bleed function so manual bleeding shouldn't be required if you follow the instructions and don't loose too much),

17) run the engine and check for leaks, and then grease and refit a new dust/dirt seal, it clicks in a groove on the input shaft with the lip in a slot on the top of the box,


18) refit the steering column, rubber boots, headlight frame and grille,

19) do a road test to exercise the steering box (carefully, the brakes are hydraulic powered as well as the steering), check for leaks and recheck the reservoir level. Do this several times over a few days.

What you need

1) An input shaft seal kit seal kit. I acquired this kit (part number TAS75/C1) from the local TRW importers, Complete Steering Australia Pty. Ltd, Phone (03) 9369 2659. They were familiar with the Oka steering box and the seal kit was around $80 delivered. This sounds a lot but it contains the seal, dust/dirt cover and new spring clip, plus a couple of other items not needed for this fix, and it's difficult to source from elsewhere.

Input Shaft Seal Kit.
2) 2 hydraulic fittings, a Ryco S56-12 or Pirtek AU-12 male plug, and a Ryco S65-12 or Pirtek AW-12 female cap, or equivalent (about $5 each). Hydraulic pressure is used to force the old seal out and these are for temporarily capping the return outlet on the box to create internal pressure, and plugging the return hose to prevent fluid loss.

Cap and Plug for the blanking off the return outlet and hose.
3) A special tool for inserting the seal. You can buy one ($US36 from the USA plus freight, assuming the J37073 is the correct size, or around $A100 quoted locally), or you can quite easily make something similar, as it's only a stepped cylinder. The TRW manual warns against using a socket to insert the seal since if you go too far it won't seal, and might require removal and disassembly of the steering box to recover it, which is a big job. However you can use a socket if you adapt one to prevent this from happening.

A long socket modified to avoid inserting the seal too deeply.
4) A couple of litres of Automatic Transmission Fluid (Dextron 111 or equivalent) to replenish the reservoir.

Modifying the seal insertion socket

You'll need a fairly deep socket, long enough internally to surround the input shaft plus a bit, and small enough in diameter to just fit inside the seal housing. A long, 1 1/8 inch A/F, or metric equivalent would suit. To that you can fit some clamps to prevent the socket from penetrating too deeply. Only 4.3 mm depth is required. You may notice that the clamps I used are actually some old Oka saddle clamps from drive shaft rear UJ's, which I opened out a bit and bolted across the socket. You could easily make some similar clamps using 3mm steel bar. I did try hose clips but they are not wide enough to sit on the seal housing and are not flush on their lower edges.

About 4.3 mm depth is required, no more.
After removing the circlip from above the old seal, I "calibrated" the modified socket by locating it over the input shaft and nipping up the clamp bolts while it was resting on the old seal. That gives it the correct depth. Make sure the clamps are then securely tightened as you don't want them to slip up during insertion of the seal and overdo things. It's better to leave things a little short than to drive the seal too deep.

Inserting the new seal

Follow the instruction above, or in the TRW documents. They are similar but I've added some practical tips. These photos may also help.

Old seal exposed after removing the circlip (or spiral spring clip in our case).
The return hose and outlet plugged.
Using the socket to insert the new seal.

(The socket was calibrated this way too with the old seal in place)

It was a little bit squeezy wielding the hammer above the inlet shaft (a slightly shorter socket would have been better), but it doesn't need too much force, and it's a good thing anyway if it prevents the seal from going in too far. In my case the seal didn't go in quite level so I had to tap the socket on one edge to level it up. The seal must only be inserted far enough for the circlip to fit fully in its slot.

The circlip located in its slot above the new seal.
After putting the new circlip in, I removed and replaced it a couple of times to ensure that it really was fully in the slot. You don't want the seal popping at the wrong moment and distributing fluid all over the Oka and road, and leaving you without steering or brakes. If the circlip is not quite in its slot, put the socket back on top of it and tap it down gently until it seats properly.

Remove the plug and cap from the return hose and quickly reconnect to the steering box, to reduce fluid loss, and tighten fully.

To aid the bleeding process, and before reconnecting the steering column shaft and lower UJ, I ran the engine several times briefly as per the instructions, checking the reservoir level in between. Ensure there are no more leaks, from the input shaft or return hose, then grease and refit the new dust/dirt cap. If all is OK, then you can fit the lower UJ and steering column shaft.

The seal and dust cap in place, with blue grease under the cap to keep out water.
Replacing the steering shaft

The steering column shaft can be replaced without disturbing the steering wheel housing but needs to be manually compressed and expanded as it's fitted to the splines at each end. It's better to leave all the pinch bolts off until the shaft and lower UJ are in place. Being able to slide the shaft up and down the spines makes fitting it a bit easier. Ensure that the steering wheel is aligned with the front wheels in the straight ahead position before assembly.

The lower UJ back in place with safety locknuts fitted.
I fitted Nyloc nuts plus extra locknuts to the UJ bolts to ensure they never, ever work loose.

When refitting the steering shaft, according to TRW, the UJ's should be in phase to avoid cyclic binding. I never knew I suffered from cyclic binding but apparently it can occur where there are 2 or more UJ's in the steering shaft and they are out of phase.

"Steering column assemblies with more than one universal joint (cardan type) can cause a cyclic binding feel or torque variation at the steering wheel if the u-joints are not in phase with each other".

I presume being "in phase" means that the UJ cross shafts are parallel, like in this photo, but they don't explain. (Note: the urethane bush clamped to the siding shaft is to reduce steering column rattle, which works well and could easily be installed at this point, see this article).

Steering shaft with UJ's in phase, I think.
Replacing the rubber boots and steel framing brackets is easier if they are first slit/cut up the back. You don't then need to slide them over one end of the steering shaft where they get in the way of reconnecting it. The steel clamps should hold them in place but they can be super-glued if you need to, or as I did, hold them together with nylon tie-wraps.

Rubber boots, slit up the back to aid assembly.

(They were cleaned before reinstallation)
I also fitted a leather boot to the the lower UJ to protect it from the worst of the dust and water.

Leather boot to protect the lower UJ.